Everybody
wants to run higher boost, because that's where all the power is hidden,
right?
That's
roughly true, but if we're trying to interfere with the sequential system,
at least we want to keep the disruption to a minimum.
Having
seen how the sequential system works, we now
appreciate the complexity underneath. The orchestration is conducted
by the ECU but the result is also determined by the performers themselves.
The way the actuators are connected to the pressure signal and
the strength of their individual springs dictate some of the
timing of the events. Also the airflow through the airpipes (especially
the 'bypassing' or 'bridging' ones) is pressure-driven, and that is
not always obvious just by looking at a diagram.
It is similar
to aerodynamics --- just because we create a duct and want
the air to flow through it, doesn't mean that under operating conditions
the air does what our common sense feels it should. Very often it does
something totally different. Pressure differences also depend on temperature
differences, not just airspeed. As air moves down a path it cools down,
especially if the path is narrow and the pipe is metal. So pressure
differences can exist even on (what appears to be) the same boost signal
path.
The Toyota
engineers had thoroughly measured, tested and debugged the original
setup, so it works 100%. But when we start restricting pipes and blocking
paths, the whole balance changes and it's not easy to foretell what
repercussions we are creating. Chaos theory for the paranoid.
Enough
theory dude, where do I fit my boost controller now? In all this maze
of hoses, pipes and actuators I don't know where to start!
The typical
point that boost controllers intercept is the one below:

The
wastegate actuator of turbo#1 is always connected to the boost signal.
So when the engine is doing 2 psi, that's what the back of this actuator
is filled with.
Or is it?
Looking closely we see another connection at the back of the actuator,
on the same side of the diaphragm. It goes back to the unpressurised
side of the intake, via the VSV.
Aye, 2 psi may be squirting through the actuator, but if the VSV is
wide open then there is a generous 'relief' path for the pressure, so
in reality the actuator never sees more than a fraction of a psi.
If the VSV has been shut by the ECU however, then the actuator will
be filled with boost gases, and will be at the same boost pressure as
the intake manifold (a bit higher actually, since it receives hot gases
before the intercooler, which have a higher pressure compared to the
manifold, where boost gauges typically get their signal from).
If
you use a 'bleed valve' it won't matter a lot if you use either of the
two pipes coming off this actuator. In both cases you'd be depressurising
(partially) the actuator. How much would depend on the position (pulse
duty-rate more accurately) of the VSV.
If
you use a 'ball and spring' boost controller then it does
matter which pipe you use. It has to be the one shown above - the 'pressurising'
one.
Electronic
boost controllers usually ask for the VSV to be blocked off so that
they can fully control the boost pressure behind the actuator. This
is normal, otherwise the ECU would be trying to undo the actions of
the boost controller, and the result would be a funny boost curve.
I've
done this mate, but I only see higher boost at high rpm, say 4Krpm upwards.
What's the vibe then?
The
vibe is that you didn't bother to read the long page on how the system
works. There are two wastegates operational until 4Krpm, the WGV and
the EBV.
They are both upstream of turbo#1.
They are also both continuously connected to the boost signal taken
from before the intercooler.
They also both have a VSV downstream which is pulsed by the ECU.
Therefore at low revs (below 4K) there are two wastegates
in the system
You
have only fiddled with the workings of the WGV, so the EBV still does
what it's supposed to do: keep max boost levels down to stock. To put
it simply, the EBV is bleeding off gases that could be used to spin
turbo #1 even harder.
Since
both of these valves operate in similar ways, we can replicate what
we did with the WGV, i.e. stick a "ball and spring" controller
on the pipe pressurising the EGV actuator. However, there are two extra
issues here:
1.
Accessibility. This actuator is tight between the engine and
the firewall, so accessing the two nipples is a fiddly job.
2.
The fact that the EBV also controls the prespooling of turbo
#2.
This is more serious, because in order to get more boost out of the
whole system at low revs, you need this valve to open later. But this
means that there will be less gases available to prespool turbo #2.
Even worse, turbo#2 will then have to jump suddenly and catch up with
the new, higher boost levels we've created. Not very straightforward
then.
An
unsatisfactory approach found on the
internet
The setup
below is easy to implement, because that intersect point is easily accessible
at the top of the engine. A 'ball and spring' controller cannot be used
here, because it is downstream of the actuator. So the only option is
a bleed valve or an electronic boost controller.
What we'll
be achieving is that the EBV VSV will be pulsed shut by the ECU, but
some of the pressure will be escaping from the bleed valve. So we're
effectively reducing the duty rate of the VSV. This is preferable, as
it gives a higher degree of fine-tuning. We do need this, because we
need a safe balance between higher boost at low revs and retaining some
prespool for the second turbo.

Unfortunately
it doesn't really work, because the return path is long and torturous
and doesn't bleed off quickly enough. This leads to the need to increase
the rate of bleeding leading to an on/off situation, where the actuator
is either under full boost pressure, or empty.
There
are other ideas floating on the internet, none of which have an advantage
to this solution (quite funny to see a bleed valve up the list of mods
for such a complicated engine!)
The
most dangerous of all is this one:
You
are 'advised' to Tee the two hoses below A and B. This gives maximum
boost at low revs.

Looking
at these locations on the vacuum diagram we see why this is dangerous.
The 'mod' totally bypasses the VSV, so any pulsing by the ECU is in
vain.
Point A is always in vacuum, from idle upwards.
Point B is usually under positive pressure, roughly at what the boost
gauge would show.

What
this means is that there will always be a rush of air from B to A and
this will be much stronger when the engine is under higher boost. Therefore
the EBV actuator will never be pressurised, and it will only open the
EBV when the backpressure after turbo #2 manages to overcome the actuator
spring pressure. While the EGCV is shut (below 4Krpm) this ain't gonna
happen any time soon.
...so the EBV will always be shut, at least until 4K rpm. This means
that the prespool for turbo #2 will be zero (save the odd pressure
leak from the EGCV or the EBV)
But
wait, it gets worse: a couple of hundred revs after the
EGCV has opened, the IACV is ordered to open, because the ECU assumes
that by that time the boost pressure created by turbo#2 is well up to
the levels of turbo #1. But that assumption is with prespooling in mind.
Without any prespooling, it will certainly take longer for turbo
#2 to catch up with #1. So we risk the ECU opening the IACV wide open
while turbo#1 produces more boost than turbo#2:

In
the example above, turbo #1 produces 11psi (pressure left of the IACV)
while turbo #2 produces 7psi (pressure right of the IACV) This is possible
while the IACV is kept shut -- note that the reed valve can only flow
the other way, so that is shut as well.
The moment the ECU orders the IACV to open, the full blast of the pressure
tank fills the IACV actuator and it tries to crack open,
since now it has to overcome the 4 psi (11psi - 7psi). Let's put aside
the extra stress of the IACV flap for now. Even if it doesn't manage
to open fully, we'll be left with higher absolute pressure on the left
of the valve, and lower on the right. No guesses as to which direction
the air will try to flow. But that is against the direction the compressor
of turbo #2 is trying to flow. So the turbine of #2 is trying to turn
in one direction, while the compressor faces a sudden brake, trying
to turn the shaft the other way. That can't be good!
This is compressor surge caused deliberately by the ill-advised 'mod'
and the stock 'dump' valve can do nothing to relieve it (apart from
being downstream of the intake 'meeting point' it would never react
anyway since its pressure reference shows 'boost').
How
long turbo #2 will survive is anyone's guess.
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There
are other variations on this theme, where the connecting pipe
between A and B is partially restricted, so that (hopefully) some
prespool will take place
--- at the expense of running higher boost at low revs of course.
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Another
hack would be to fit a bleed valve on pipe B and adjust carefully, slightly
increasing the leak and checking on the road and boost gauge that only
a couple of psi have been gained over stock. This might keep some prespool
and hopefully find a happy mid-point where turbo #2 won't be kicked
to work from a total idle state, then be surged to death.
What
all the above methods fail to do is intercept the EBV pressurising signal
(seen below)

That's
something that has to be done. It's fiddly but not impossible.
A
better way to increase low-rpm boost
An
internet favourite is Stuart
Hagen's EBV mod.
This is a bit more involved to implement. You need to crawl between
the firewall and the back of the engine and disconnect the vacuum hoses
from the EBV actuator. You then run a new hose (after blocking off one
of them) and connect it to the pressure tank feed --- by using a "Y"
splitter at the top of the engine. This creates a new path to the pneumatic
activation of the EBV, so a boost controller can be used to open the
turbo#2 prespool whenever we like. (The EBV VSV is also blocked off)
This
mod allows max boost at low revs, well over 1 bar is possible. If a
ball&spring valve is used, then it should be set to open at least
3-4psi below the system's max boost setting on the wastegate, allowing
allowing some prespool. (local copy here)
An
even better way to increase low-rpm boost
This
is my favourite, a variation on the theme of the previous 'EBV mod'
Again,
access to the EBV actuator is quite restricted by the firewall, you
may wish you had fingers like Edward Scissorhands.
Let's put it this way: if Chopin had a Supra, all his friends would
go to his place to get the EBV mod done.
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First
there is a water pipe and an air pipe (idle control circuit) that
need to get out of the way. Thankfully the coolant leaks will
be minimal as this pipe is at the highest part of the engine.
The
electric loom for the two VSVs has to move on the side, too. Easy.
Then
you stare wondering Matrix-style: "is it hose #1 or hose
#2 that I need to pull off?"
The
answer is "neither!".
These
hoses are irrelevant to the EBV mod, although they'd be convenient
if they indeed went to the back of the EBV actuator, as they appear
to do.
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Under
closer inspection and by using a bright torch you see the two
hoses coming off the actuator.
As
we're looking down the firewall, the one to the right is the 'feed',
we can see the "T" junction of the pressurised metal
feed as it goes to the pressure tank.
The
one to the left is the 'relief', which the EBV VSV pulses open
according to the ECU's commands. The more it's pulsed open, the
more boost is leaked back into the pre-compressor intake and the
EBV actuator is forced to close again.
Note
that in this diagram view pressure to the left, relief to the
right. Don't mix them up, we leave the relief alone.
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Here
we can see some long-nosed pliers that will help cut down on bad
language as we try to negotiate hoses and clips hidden down the
firewall...
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In
an ideal world we'd keep the original EBV actuator feed and relief
performing the same tasks. We'd just want to insert a Manual Boost
Controller (MBC) in the feed so that it doesn't flow anything
below a preset pressure level (say 1 bar)
That's
exactly what we're going to do.
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Apart
from various lengths of vacuum hose, we need two connectors a
"T" and a "I".
Make
sure that their dimensions are proper for the internal diameter
of the hoses used. You don't want them too thick (they won't fit,
and you may not even be able to push the "I" inside
the remote feed) and you certainly don't want them too thin (they'll
pop off)
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Here
is the "T" junction that has been introduced to the
original boost feed.
It
still feeds the metal pipe as it used to (ultimately ending up
to the pressure tank) and now it also feeds our rendition of EBV
actuator control
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1.
Hose coming from the EBV actuator's pressure side. No need to
take off the old one completely, just undo it from the metal hose
and use the "I" connector to extend it. Don't forget
to block the metal ending ofcourse.
2.
MBC ensuring that boost only pressurises the actuator when it
exceeds the limit we set
3.
"T" connector diverting boost pressure towards our new
EBV boost feed.
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Another
view of the same setup.
1.
MBC
2.
"T" junction
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The
beauty of this setup is that the EBV relief is still intact, so the
ECU still has partial control of the EBV. If it tries to pulse the VSV
at boost pressure below our MBC setting, obviously nothing will happen
because the actuator is empty.
But if it tries to pulse the actuator above our setting, it will work
fine! So if at high boost (over 1bar and over 4Krpm) the ECU wants to
shut the EBV actuator, now it can do so. Also if during a downshift
it decides to open the EBV it can still do something, it's not castrated
as it is with the previous plumbing.
As
a bonus, it's very easy to turn the setup back to standard --- just
eliminate the MBC, or take out the ball and spring and refit the adjusting
screw.
The
results obviously depend on the settings of the MBC. A logical setting
would be to have it set to 15psi for example, and the wastegate set
to over 15psi via another MBC.
Then
at low revs (up to around 3800)turbo #1 will hit a boost level of 15psi
and stay there (the excess gases will be prespooling turbo #2). At around
3800rpm overall boost pressure will drop a few psi as the second turbo
comes fully online, then it will shoot up to whatever level the wastegate
MBC is set to.
If
the EBV MBC is set to 13psi, then turbo #1 will hit 13psi boost, and
the drop at 3800rpm will be less obvious, as more gases were allowed
to prespool turbo #2 and the 'gap' from #1 was not so wide this time.
There
is some fine-tuning to be done with the newly-installed EBV MBC, don't
be greedy, start from a low boost level and gradually go upwards until
the 3800rpm boost drop becomes an issue.
Stealthy
version of this mod
The
"T" piece right in front of the engine is a giveaway that
the engine is not stock. This can be avoided easily for those who like
sleepers, or the 'factory' look.
First
of all don't use blue silicon hoses, rather black fuel hoses. They are
bound to attract less attention and be at least as durable under the
harsh engine bay environment.
Second
you can completely avoid the "T" at the front and extend the
stock EBV actuator metal feed via another hose (instead of blocking
it off and using the "T" described above). The MBC could be
secured with cable ties near the firewall and nobody would be any the
wiser.
Technically
it is exactly the same thing, there is no reason to prefer one approach
to the other.
Faster
spoolup too - as a bonus!
An
interesting by-product of the above modifications is that the car builds
boost quicker overall.
It
feels faster, and that's because if you use MBCs on both
actuators (remember at low revs turbo #1 thinks it has TWO wastegates)
no boost whatsoever enters these actuators until 1 bar is reached (or
whatever the lowest setting is for any of the two). Therefore ALL exhaust
gases are available to turbo #1 until the very last moment, when the
EBV actuator is filled with boost and opens up.
One
would expect the ECU in stock form to do the same thing - i.e. keep
these actuators free from boost until the preset level are reached,
then pulse them opened. That's what the VSVs are there for. But in real
life, standard ECUs are programmed to be smooth and gentle, so they
start pulsing the actuators open well before the full settings have
been reached, diverting exh gases that could be better used to spool
up the turbos quicker.
By
using MBCs on both actuators this 'smoothness' is gone. Note that if
you use an MBC on just one actuator you won't feel any difference, because
the other one still diverts gases before their time. You need MBCs on
both wastegate and EBV to get this extra edge in spoolup.
Yikes
dude, I didn't understand half of the stuff you've said, but now I'm
kinda scared.
Makes
you think twice before changing anything off-standard, doesn't it?